On the Friday everything went well and the van drove fine despite the M25 traffic and we got the layout erected that evening, but again there was no time to test it.
On the Saturday we arrived as early as possible and began to test. Nightmare! The dreaded short circuit problem was back. It took us over 2 hours to find the problem having isolated the issue to the platform board - 4 bits of straight track, how could that be the problem? After much re-gapping of copper clad sleepers and other investigative work I took the decision to start unsoldering feeds to try and find the problem. The first two wires I unsoldered fixed the problem! We still don't know the cause of the problem but suspect that it was to do with copper clad sleepers touching at board joins, the unsoldered feed meaning it must have been the long siding.
All this meant that the first time a loco made it around the layout was a grand 4 minutes before the exhibition opened to the public!
All this also meant that the time we had put aside to add decoders and test a couple of other locos was lost - no Merddin, 138 or 87 - sorry!
Having now got the beast home, I have found that the motor is dead - how unlucky is it for that to happen during the exhibition!
There are a number of areas where learnings from the grand test will be enacted though:
- The alignment at the north end of the platform is too complex, mainly caused by swapping from crazy to mainline peco points. This needs much more thought and at the moment I expect that I will extend the board by a foot or so and straighten out the end of the platform so that the curves out of the station are more manageable and the board joins are much closer to parallel to the board edge.
- The N gauge points in the hidden sidings struggled, especially the farish ones and fettling/replacement will be necessary plus proper testing(!)
- Certain carriages need greater gaps between adjacent carrs and changes to their pivots which on some do not allow the bogies to swivel easily enough. Washers, filing and a bit of oiling can solve this.
- Some vehicles need extra weight, but we also need to be careful about the total weight of trains, as Vale of Ffestiniog couldn't pull 5 WHR saloons up the gradients on the layout.
I would like to thank many readers of this blog and others who commented on the scenery and stock despite the running issues. Indeed it appears that railway modeller are interested in featuring the layout in a future issue too, so it must have looked alright. I was delighted by how it has turned out and was also pleased that the structure of the layout worked well, the overall lighting was good, the station lamps and point indicator lights worked well and generally the tortoises did their job. We also managed to take the layout down and pack it away in about an hour, which I thought was good for a layout of this size.
It's hard work an exhibition, and I have much respect for those who do it often, I suppose this one was especially hard for us given the problems, but a team of 4 worked well and we all got to see a bit of the exhibition too.
So I shall now be taking a break from 009 as I start a new job tomorrow. Any spare time until Christmas will be used to further 16mm projects, notably the De Winton before I return to 009 in the new year.
I had a number of enquiries about other exhibitions, but really want to put right a lot of the issues found and that will take time. I expect therefore to next show Rhyd Ddu in Spring 2012.
Here are some other shots:
oooh 7mm FR stuff!........
and some shots of locos that didn't quite make it...here's 87's body:
and Merddin:
and some more shots here: http://www.flickr.com/search/?q=rhyd&w=16967289%40N02
and here: http://campbell-modelrailway.fotopic.net/c1911735.html
see you in the new year!
Colin
4 comments:
Exhibitions are a trial by fire for even the most established layout. You've achieved a hell of lot to get to where you have and it can only get better! Looking forward to seeing it again.
Good to meet you Colin, and see that first train round ...! It looked a bit frantic first thing but running nicely when I passed later in the day. A great effort to get there, layout and stock looked fantastic.
Hi Colin,
Congrats with the first official and public performance of the layout!!
You (and your father) achieved an astonishing lot in the last few months!
Well done Colin, you've achieved a lot in a relatively short space of time! It was nice to meet you, and the layout having read about it for some time now.
As I said, it looks pretty enough to distract from when people run odd stock combinations when you're not looking!
Looking forward to seeing what the blog will contain now it's 'finished'!
Congrats on the potential RM feature too!
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